Nuclear Update

Peach Bottom:

 

May 13, 2011 – The NRC said there would be no significant environmental impact with the transfer of low-level radioactive waste from the Limerick Generating Station in southeastern Pennsylvania to a storage facility at the Peach Bottom plant.

 

Peach Bottom officials initially requested a license amendment to allow the transfer of the waste on Jan. 6, 2010. The waste does not include any transfer of spent nuclear fuel from Limerick.

 

Exelon operates both nuclear power plants.

 

The Limerick plant does not have the capacity to store all of the low-level radioactive waste it generates. The NRC noted that the Barnwell disposal facility in South Carolina is no longer available for Limerick, but Peach Bottom has the ability to store a large amount of low-level waste on an interim basis.

 

In its environmental analysis, the NRC noted that there would be two or three shipments a year from Limerick to Peach Bottom. “The distance between the plant sites is less than the distance that was previously traveled to the Barnwell disposal facility in South Carolina,” the NRC noted.

 

“The staff concludes that the radiological impacts associated with the transportation, handling and storage of low-level radioactive waste at Peach Bottom will not result in a significant impact to plant workers and members of the public,” the NRC said.

 

“The proposed action will not significantly increase the probability or consequences of accidents. No changes are being made in the types of effluents that may be released offsite. There is no significant increase in the amount of any effluent released offsite. There is no significant increase in occupational or public radiation exposure. Therefore, there are no significant radiological environmental impacts associated with the proposed action.”

 

 

Berwick plant

 

May 16, 2001 – Operators of the Susquehanna nuclear plant near Berwick shut down the Unit 1 reactor for an inspection of the main turbine.

 

The precautionary shutdown was done to inspect the blades of the turbine. Workers detected defects on similar blades in the Unit 2 turbine during a routine inspection as part of a refueling and maintenance outage.

 

Officials said the defective turbine blades on Unit 2 are being replaced. Unit 1 will be returned to service when the inspection and any needed repairs are completed, PPL officials said.