TMI Update: Jan 14, 2024


Did you catch "The Meltdown: Three Mile Island" on Netflix?
TMI remains a danger and TMIA is working hard to ensure the safety of our communities and the surrounding areas.
Learn more on this site and support our efforts. Join TMIA. To contact the TMIA office, call 717-233-7897.

    

U.S. Nuclear Regulatory Commission
Operations Center
 
EVENT REPORTS FOR
05/17/2022 - 05/18/2022
 
55899
Power Reactor
Event Number: 55899
Facility: Peach Bottom
Region: 1     State: PA
Unit: [2] [] []
RX Type: [2] GE-4,[3] GE-4
NRC Notified By: Linell, Bill
HQ OPS Officer: Brian P. Smith Notification Date: 05/16/2022
Notification Time: 19:51 [ET]
Event Date: 05/16/2022
Event Time: 15:52 [EDT]
Last Update Date: 05/16/2022 Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical
50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation Person (Organization):
Lilliendahl, Jon (R1DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 A/R Y 100 Power Operation 0 Hot Standby
Event Text
AUTOMATIC SCRAM DUE TO ELECTRICAL TRANSIENTS
 
The following information was provided by the licensee via fax:
 
"Unit 2 experienced multiple electrical transients resulting in a Group I Primary Containment Isolation Signal (PCIS) isolation and subsequent unit reactor scram. Low reactor water level during the automatic scram caused PCIS Group II and III isolation signals. Following the PCIS Group I isolation, all main steam lines isolated. All control rods inserted and all systems operated as designed."
 
The following additional information was obtained from the licensee via phone in accordance with Headquarters Operations Officers Report Guidance:
 
Peach Bottom Unit 2 automatically scrammed from 100 percent power due to an electrical transient and subsequent PCIS Group I isolation (Main Steam Isolation Valve closure). Unit 2 lost main feedwater due to the PCIS Group I isolation, however, all other systems responded as expected following the scram. High Pressure Coolant Injection is maintaining pressure control while Condensate Pumps are maintaining inventory. The unit is currently stable and in Mode 3. Peach Bottom Unit 3's Adjustable Speed Drives were impacted by the electrical transients and the unit reduced power to 98 percent power.
 
The NRC Resident Inspector was notified.
U.S. Nuclear Regulatory Commission
Operations Center
 
EVENT REPORTS FOR
05/17/2022 - 05/18/2022
 
55899
Power Reactor
Event Number: 55899
Facility: Peach Bottom
Region: 1     State: PA
Unit: [2] [] []
RX Type: [2] GE-4,[3] GE-4
NRC Notified By: Linell, Bill
HQ OPS Officer: Brian P. Smith Notification Date: 05/16/2022
Notification Time: 19:51 [ET]
Event Date: 05/16/2022
Event Time: 15:52 [EDT]
Last Update Date: 05/16/2022 Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical
50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation Person (Organization):
Lilliendahl, Jon (R1DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 A/R Y 100 Power Operation 0 Hot Standby
Event Text
AUTOMATIC SCRAM DUE TO ELECTRICAL TRANSIENTS
 
The following information was provided by the licensee via fax:
 
"Unit 2 experienced multiple electrical transients resulting in a Group I Primary Containment Isolation Signal (PCIS) isolation and subsequent unit reactor scram. Low reactor water level during the automatic scram caused PCIS Group II and III isolation signals. Following the PCIS Group I isolation, all main steam lines isolated. All control rods inserted and all systems operated as designed."
 
The following additional information was obtained from the licensee via phone in accordance with Headquarters Operations Officers Report Guidance:
 
Peach Bottom Unit 2 automatically scrammed from 100 percent power due to an electrical transient and subsequent PCIS Group I isolation (Main Steam Isolation Valve closure). Unit 2 lost main feedwater due to the PCIS Group I isolation, however, all other systems responded as expected following the scram. High Pressure Coolant Injection is maintaining pressure control while Condensate Pumps are maintaining inventory. The unit is currently stable and in Mode 3. Peach Bottom Unit 3's Adjustable Speed Drives were impacted by the electrical transients and the unit reduced power to 98 percent power.
 
The NRC Resident Inspector was notified.
Dear CIS & Decommissioning Working Groups,
05/10/22
9:00AM -
12:00PM ET
Peach Bottom Atomic Power Station, Units 2 and 3 - Integrated Inspection Report 05000277/2022001 and 05000278/2022001

ADAMS Accession No.  ML22117A036
 
Zip of three placed into ADAMS today
 
 
Three Mile Island Unit 1 Issuance of Amendment 304 to Revise License Conditions and the Permanently Defueled Technical Specifications to Align rqts for Permanent Removal of Spent Fuel from Spent Fuel Pool
 
N2
MJK
DEP Newsroom
 
COMMONWEALTH OF PENNSYLVANIA
Dept. of Environmental Protection

Commonwealth News Bureau
Room 308, Main Capitol Building
Harrisburg PA., 17120

 
FOR IMMEDIATE RELEASE
04/22/2022
 
CONTACT:
Neil Shader, DEP
717-787-1323

 
Pennsylvania Enters the Regional Greenhouse Gas Initiative
Participating in the multi-state initiative will cut pollution and fight climate change

 
Harrisburg, PA – The Wolf Administration has finalized the regulation to combat climate change and allow Pennsylvania to participate in the Regional Greenhouse Gas Initiative (RGGI), fulfilling a promise made in a 2019 Executive Order to take part in the market-based program.
 
“Today we are already experiencing the effects of climate change and those impacts are only going to get worse. Our children and their children are going to look back at our decisions and by participating in RGGI, we have begun to set Pennsylvania on the path forward to addressing this threat,” said Department of Environmental Protection (DEP) Secretary Patrick McDonnell. “Climate change caused by pollution remains the most critical environmental threat confronting us and we are already paying the price.”
 
DEP’s CO2 Budget Trading Program regulation, which will enter Pennsylvania into RGGI, will be published in the April 23, 2022 issue of the Pennsylvania Bulletin.
 
“This regulation has the support of businesses and residents, and will save lives and millions of dollars by cutting air pollution,” said McDonnell. “This is only one step necessary to fight climate change, and while Pennsylvania cannot singlehandedly solve the global climate crisis, the world cannot solve the crisis without Pennsylvania.”
 
Some of the benefits of RGGI for Pennsylvania include:
• Reducing up to 225 million tons of carbon pollution from Pennsylvania power plants by 2030
• Preventing up to 30,000 hospital visits for respiratory illnesses like asthma
• An increase in Pennsylvania’s Gross State Product of nearly $2 billion, and a net increase of 30,000 jobs by 2030
 
Nearly 14,000 people commented on the regulation, including the hundreds that participated in the 10 virtual public hearings DEP held. Throughout the regulatory process, DEP held over 15 public discussions on the regulation with a range of expert advisory committees. The final regulation was supported by both the Citizens Advisory Council and the Air Quality Technical Advisory Committee.
 
“The reaction from Pennsylvanians during the development of this regulation was clear – they want us to take action on climate. Communities and businesses are already experiencing the impacts of climate change, and those impacts will only accelerate between now and 2050. Most Pennsylvanians realize we need to do something about that,” said McDonnell. “Reducing the carbon pollution that drives climate change is critical to preventing some of the worst impacts of climate change.”
 
“RGGI is also important for environmental justice communities,” said McDonnell. “The initiative creates a financial incentive to reduce carbon pollution to which environmental justice communities are often more vulnerable due to social and economic factors. Communities facing environmental justice issues are likely the first communities to feel the effects of climate change through heat waves and flooding, while also likely being communities with the fewest financial resources to adapt.”
 
RGGI is an initiative of 11 New England and Mid-Atlantic states that began in 2009 to reduce greenhouse gas emissions from the power sector while generating economic growth. Together Connecticut, Delaware, Maine, Maryland, Massachusetts, New Hampshire, New Jersey, New York, Rhode Island, Vermont and Virginia cap and reduce their power sector carbon dioxide (CO2) emissions. This is achieved by setting a regional cap or limit on CO2 emissions from electric power plants in the participating states. That cap decreases year over year to reduce overall carbon emissions. Pennsylvania’s participation will increase the size of the program approximately 40 percent.
 
Qualifying power plants must acquire CO2 allowances equal to the amount of CO2 they emit. And while each state has its own allowance budget, the only firm cap is the regional one. Entities in each of the qualifying states can purchase and trade allowances- allowing for the most efficient and cost-effective emissions reductions. Also, since RGGI is a market-based approach, the quarterly auction sets the price for the purchase of allowances to ensure transparency.
 
DEP will now determine the number of allowances for carbon pollution required for each power plant. Power plants must start accounting for their CO2 emissions starting on July 1, 2022. Facilities have until March 1, 2023, to account for 50 percent of their 2022 emissions and until March 1, 2024, to account for 100 percent of their 2022 emissions. Power plants will be required to have 50 percent of their 2022 required allowances by March 1, 2023, and 100 percent of required allowances by March 1, 2024.
 
More information is available at www.dep.pa.gov/rggi
Nuclear Regulatory Commission - News Release
No: III-22-006 April 21, 2022
Contact: Viktoria Mitlyng, 630-829-9662 Prema Chandrathil, 630-829-9663
 
NRC Issues Confirmatory Order to the Department of Veterans Affairs
 
The Nuclear Regulatory Commission has issued a Confirmatory Order to the Department of Veterans Affairs documenting an agreed upon set of actions to address two apparent violations of NRC requirements.
 
The apparent violations occurred when a nuclear medicine technician at the VA Greater Los Angeles Healthcare System facility deliberately failed to complete a required test and falsified records related to that test. The VA holds a Master Materials License from the NRC, which authorizes federal organizations to use nuclear material at multiple sites.
 
The organization’s officials requested the NRC’s Alternative Dispute Resolution process, where a neutral mediator assists the NRC and its licensee in reaching an agreement regarding the corrective and preventative actions to be taken by the organization. The NRC could refrain from issuing a Notice of Violation or a Civil Penalty for the apparent violations.
 
The Order documents the commitments made by the VA following the March 2, 2022, ADR mediation session. The commitments include conducting a nationwide anonymous safety culture survey of VA employees working with nuclear materials; conducting safety culture training; and re- energizing the VA’s employee concerns program related to reporting of radioactive program allegations or adverse events.
 
The agency’s Dec. 2, 2021, investigation report describes the circumstances of the apparent violations and the VA’s actions following the incident.
 
‘The Meltdown: Three Mile Island’ Trailer: An Explosive Atomic Conspiracy Is Untangled
The worst nuclear event in U.S. history took place on Three Mile Island in Middletown, PA, in 1979, and now a new Netflix documentary revisits what exactly went wrong.

Samantha Bergeson
Apr 19, 2022 10:31 am
 
The Meltdown"The Meltdown: Three Mile Island”
Netflix
 
A four-part Netflix documentary sheds new light on the staggering effects of the near-catastrophe at the Three Mile Island nuclear power plant in 1979.
 
The Middletown, Pennsylvania-based plant suffered a breakdown in 1979, and series “Meltdown: Three Mile Island” reexamines the series of missteps that led to the national cover-up. Academy Award–nominated director Kief Davidson (“The Ivory Game”) collaborates with “Erin Brockovich” producers Michael and Carla Shamberg and Moxie Pictures to tell the true story of what happened at Three Mile Island’s “first step in a nuclear nightmare,” as the trailer states. “Meltdown” premieres May 4.
 
The four-part documentary reveals how it all unfolded in real time, the impact on the community, and the personal account of chief engineer and whistleblower, Richard Parks, who had the courage to speak up and prevent a near catastrophe for the East Coast. Dramatic reenactments, archival footage, never-before-seen home video, and in-depth interviews bring viewers into the worst nuclear incident in U.S. history.
 
From radioactivity seeping into the control room to plant operatives hiding the nuclear disaster from the general public, the events behind “Meltdown” are of a staggering conspiratorial scale. The accident was the partial meltdown of an atomic reactor in March 1979, marking the most significant accident in U.S. commercial nuclear power plant history. But was the accident preventable?
 
“I believe the lessons of ‘Meltdown’ resonate far beyond the events of 1979,” said director Davidson, who also serves as an executive producer. “Even as we expose the complex web of corporate greed which nearly led to our radioactive ruin, we find the small acts of bravery that changed the course of history. We need to learn from the Three Mile Island disaster as we face the current climate and energy crisis.”
The plant’s parent company, Metropolitan Edison, reportedly downplayed the crisis and claimed no radiation had been detected off plant grounds. However, inspectors tracked increased levels of radiation as well as a contaminated water leak.
 
Executive producers Carla and Michael Shamberg added, “Whistleblowers are real-life superheroes. They risk their lives or livelihoods when they speak truth to power to protect the rest of us.”
 
Robert Fernandez and Dan Levinson also executive produce.
 
“Meltdown: Three Mile Island” premieres May 4 on Netflix. Check out the trailer below.
 

Dismantlement work at San Onofre nuclear facility halted after worker injury

Crews work on the demolition of                    the San Onofre Nuclear Generating Station.
Crews work on the demolition of the San Onofre Nuclear Generating Station. 
(Nelvin C. Cepeda/The San Diego Union-Tribune)

 

Contract worker hurts shoulder after falling about 5 feet.

BY ROB NIKOLEWSKI

APRIL 18, 2022 3:50 PM PT

Work on dismantling the San Onofre Nuclear Generating Station has been on hold for the past week after a worker on April 11 fell about 5 feet into an open space in one of the rooms primed for demolition, injuring the worker’s shoulder.

The worker was taken to a nearby hospital and released, and officials at Southern California Edison — the operators of the now-shuttered plant known as SONGS for short — put a stop to all dismantlement efforts to start an investigation. An Edison spokesman told the Union-Tribune on Monday demolition “not directly related” to the work where the incident occurred may resume later this week.

“It is important for us as an organization to fully understand what happened, what may have led up to the incident and, ultimately, how these safety events can be prevented in the future,” Edison vice president and chief nuclear officer Doug Bauder said in a statement.

The accident involved two contract workers hired by SONGS Decommissioning Solutions, the general contractor chosen by Edison to take down nearly all of the structures on the 84-acre site between Interstate 5 and the Pacific Ocean.

According to Edison, work was being done on an equipment vault, an enclosed room that is below floor-level inside the Radiological Control Building at SONGS that contained abandoned equipment that needed to be removed.

Two workers were tethered together by safety harnesses while trying to install a ventilation hose into the floor vault opening. When one worker lost balance, the other tried to catch the person from falling and fell about 5 feet into the vault, resulting in the shoulder injury.

If not restrained by the safety equipment, the workers could have fallen as far as 25 feet.

Officials with SONGS Decommissioning Solutions — a joint venture of Los Angeles-based engineering company AECOM and a Salt Lake City firm called Energy Solutions that specializes in disposing of nuclear material — immediately stopped work after the incident to start an evaluation. Edison formally extended the stand-down order, the utility spokesman said, to conduct a detailed investigation and implement potential corrective actions.

As per regulations, the incident was reported to Cal-OSHA. The accident did not require reporting to the U.S. Nuclear Regulatory Commission but Edison officials say they notified the agency’s regional office.

While demolition has been halted, other decommissioning work at SONGS continues, such as radiation monitoring and general maintenance.

This past weekend, workers completed the transfer and storing of a waste canister that was moved from the plant’s Unit 2 wet storage pool to a dry storage facility at the north end of SONGS.

The canister is the first of 12 that will be moved. Combined, the 12 will hold 125 tons of radioactive material classified as “greater than Class C low-level waste.”

The SONGS dismantlement project is in the third year of an effort estimated to take about eight years to finish and cost roughly $4.5 billion. By completion, about 1 billion pounds of equipment, components, rebar, concrete, steel and titanium will be moved out of the plant. About 80 percent of the material is considered radioactive.

 

Mounds                            of crushed concrete stack near Unit-3 before                            it is hauled out. (Nelvin C. Cepeda / The                            San Diego Union-Tribune)
Mounds of crushed, non-contaminated concrete near Unit 3 at the San Onofre Nuclear Generating Station in November 2021, awaits being shipped out. 
(Nelvin C. Cepeda/The San Diego Union-Tribune)

 

The vast majority of the plant’s debris is labeled Class A waste, the lowest level of radioactive material. Most of the rubble will go to a disposal facility in Clive, Utah — primarily shipped by rail car, although some material will be transported in casks by truck. Class B and C low-level waste gets sent to a site near the town of Andrews in West Texas. Non-radioactive material goes to Arizona.

Last summer, an incident occurred in the Unit 3 containment dome but resulted in no injuries. Edison officials reported a 60-pound seismic lug from a safety injection tank fell about 18 feet to the floor after it was cut from the tank. Workers were in the area but the falling lug did not hit any of them.

Before the dismantlement project started, the Nuclear Regulatory Commission fined Edison $116,000 after a 50-ton canister filled with fuel assemblies being lowered into a newly-constructed dry storage facility in August 2018 was left suspended on a metal flange about 18 feet from the floor of its storage cavity, unsupported by rigging and lifting equipment.

The canister was eventually lowered safely but the NRC chided Edison officials for not reporting the incident within 24 hours. The NRC did not assign a civil penalty for that violation. Word of the suspended canister was not initially disclosed by Edison but by an industrial safety worker at the plant during a community meeting.

The news of the last week’s worker injury concerns Ray Lutz, national coordinator for the advocacy group Citizens’ Oversight and a frequent Edison critic.

“Everybody’s worried about, are they handling this (dismantlement) work correctly and this only makes us worry more that they are not taking proper precautions,” Lutz said. “I would be interested to see what the results of their inquiry are and I hope they have full transparency in what they release.”

Edison spokesman John Dobken said in the utility’s oversight role, “it is fundamental that we ensure a safe work environment for all employees and that is what we are doing through this pause in work and thorough review.”

Prior to the injury, SONGS Decommissioning Solutions had gone more than 2.6 million man-hours — more than a year and a half — without any event that would have resulted in workers missing work.

---------
Ray Lutz
Citizens' Oversight Projects (COPs)
619-820-5321

Pages