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From the NRC (ML100260293):

By letter dated August 7, 2008,1 as supplemented by letter dated May 7, 2009,2 Exelon Generation Company, LLC (Exelon) applied for an amendment to the Peach Bottom Atomic Power Station, Units 2 and 3, Facility Operating License Nos. DPR-44 and DPR-56. The proposed amendment consisted of several changes including the incorporation of Technical Specification Task Force (TSTF) Traveler 363, Revision 0, "Revise Topical Report References in ITS [Improved Technical Specifications] 5.6.5, COLR [Core Operating Limits Report]." TSTF Traveler 363, Revision 0, would amend the Technical Specifications (TSs) to relocate Topical Report revisions and date citations from the TSs to the COLR. The license amendment request submitted by Exelon was consistent with TSTF Traveler 363, Revision 0, which had been accepted by the NRC staff for use in licensing applications.

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From Nuclear Street:

Even as the agency considers new licensing applications, the NRC must stay focused on its core mission of ensuring the safety and security of existing reactors. No one – not the Commission, the staff or the licensees – can afford to be lulled into a sense of complacency about these issues. It was precisely this concern that motivated the Commission to create the Office of New Reactors, so that NRR could maintain a single-minded focus on the safety of the current operating fleet.

We have a lot of work ahead of us. NRR faces some long-standing challenges and some really difficult issues. Those include buried piping, submerged cables, containment sump performance, and, of course, fire protection. These issues won’t be resolved overnight. They undoubtedly will require the sustained focus of both the Commission and the staff. But we must continue to work towards closure of these issues.

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From Investigative Reporting Workshop:

The Obama administration may soon guarantee as much as $18.5 billion in loans to build new nuclear reactors to generate electricity, and Congress is considering whether to add billions more to support an expansion of nuclear power.

These actions come after an extensive decade-long campaign in which companies and unions related to the industry have spent more than $600 million on lobbying and nearly $63 million on campaign contributions, according to an analysis by the Investigative Reporting Workshop at American University.

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From the NRC (ML100280714):

This refers to the inspection completed on September 30, 2009, at Susquehanna Steam Electric Station Units 1 and 2 (Susquehanna). The purpose of the inspection was to examine activities complted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. During the inspection, the NRC reviewed two instances ofa failure by PPL Susquehanna, LLC (PPL) to obtain NRC approval for two senior reactor operators (SROs) to continue to conduct NRC-licensed activities after each SRO did not meet a specific medical prerequisite for performing the duties of a licensed operator, as required by 10 CFR 55.3. These faiulres, which were identified by your staff, were discussed during an exit meeting that Mr. Paul Krohn and the Susquehanna resident inspectors held with your staff on October 9, 2009. The apparent violation was described in detail in the subject NRC inspection report dated November 13, 2009.

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From the Rutland Herald:

The Vermont Public Service Board said Wednesday Entergy Nuclear may have provided false information to state utility regulators and the Legislature "for an extended period of time," and said the issue is "broader" than just buried radioactive pipes at Vermont Yankee.

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From the Burlington Free Press:

“Like many Vermonters, I have lost trust in the current management team, and I have been disappointed that changes have not already been made,” Douglas said during a news conference Wednesday, shifting from his long-standing support of the plant.

Douglas said long-term decisions about the plant cannot be made until the company re-establishes the public’s trust following revelations this month that the radioactive isotope tritium is leaking from the plant, and that company officials misled the state about the presence of pipes that might be involved in the leak, the source of which remains unknown.

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From Seven Days:

John Dillon spelled it out last week on Vermont Public Radio: Nuclear engineer Arnie Gundersen alerted the Public Service Department last summer that Entergy had likely lied to a special legislative oversight panel and state regulators about the existence of underground pipes — pipes that could be the source of previously undisclosed contamination.

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From LancasterOnline.com:

Exelon Energy wants to begin sending low-level radioactive waste from its Limerick nuclear plant to the Peach Bottom nuclear plant in York County.

Exelon has applied to the U.S. Nuclear Regulatory Commission to amend its operating license so that each year it can send one or two truckloads of the waste from the Montgomery County plant to Peach Bottom, where it would be stored.

For decades, most low-level radioactive waste generated at nuclear plants in the East has been sent to a licensed low-level radioactive waste facility near Barnwell, S.C.

But in July 2008 the facility stopped accepting waste from all but three states.

The on-site storage facility at Limerick is filling up, but 98 percent of the storage capacity at Peach Bottom is available for use, said Rochelle Benson, an Exelon spokeswoman at Peach Bottom.

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From the Brattleboro Reformer:

Two weeks ago, Yankee revealed a test well on site showed elevated levels of tritium in groundwater. The monitoring well showed levels of tritium ranging between 14,000 and 28,100 picocuries.

The source of the tritium has not yet been determined, but it was during the initial investigation that regulators learned there was in fact buried piping in use at the power plant.

Last week, during a search for the source, Yankee engineers discovered more than 200 gallons of contaminated water in a 40-foot-long pipe trench in the plant’s radiation waste building.

The water was found to be contaminated with up to 2 million picocuries per liter of tritium, 13,000 picocuries per liter of cobalt-60 and 2,460 picocuries per liter of zinc-65.

The Environmental Protections Agency’s drinking water limit for cobalt-60 is 100 picocuries per liter and for zinc-65 is 300 picocuries per liter.

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Good afternoon!

In case you're interested, NRC's Office of Nuclear Security & Incident Response is hosting a public meeting on proposed enhancements to the Force-on-Force Inspection Program and Significance Determination Process on February 10, 2010 from 10 am to 4 pm.

For this meeting, we will be using Microsoft Live Meeting, the same web conferencing technology used during the emergency preparedness rulemaking meetings last summer and fall. Stakeholders interested in participating via the web or over the phone should contact F. Paul Peduzzi or Raymond Gibson (contact information below) no later than February 8.

Meeting Contacts:

F. Paul Peduzzi, NSIR/DSO
301-415-5734, NSIRContact.Resource@nrc.gov
Raymond Gibson, NSIR/DSO
301-415-7801, NSIRContact.Resource@nrc.gov

Thank you!

Sara K. (Sahm) Mroz
Communications and Outreach
Office of Nuclear Security and Incident Response
US Nuclear Regulatory Commission
301-415-1692 (direct)

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